SITCOMTN-088

Summary of M1M3 Tests#

Note

This technote is a work-in-progress.

Abstract

This technote summarizes the M1M3 dynamic tests and corresponding technotes in the context of glass safety as of June 4th 2024.

Introduction#

This technote summarizes the M1M3 dynamic tests in the context of Glass Safety. It will be periodically updated with new results. The current technote corresponds to status as of June 4th 2024. A list of technotes with their updated dates and associated data sets is provided below. Following that, the list is broken down into thematic sections on different aspects of M1M3 Glass Safety and a summary of current results and next steps is provided.

M1M3 Performance Analysis#

Index of tests and verification#

Data taken on

Latest revision

Results presented in

31 May 2023
24 July 2023

SITCOMTN-079

31 May 2023 -
27 June 2023
25 March 2024

SITCOMTN-081

26 May 2023 -
20 June 2023
17 November 2023

SITCOMTN-082

01 November 2023 -
15 January 2024
31 May 2024

SITCOMTN-083

10 January 2024 -
12 January 2024
30 January 2024

SITCOMTN-084

TBC
02 November 2023

SITCOMTN-092

20 December 2023
25 February 2024

SITCOMTN-095

20 December 2023 -
22 December 2023
18 March 2024

SITCOMTN-107

04 January 2024
06 January 2024
01 March 2024

SITCOMTN-109

Force balance tests#

  • SITCOMTN-079 M1M3 Iterative Improvement of LUT Through Balance Forces

    Results: After the improvements made in July 2023 to the Look-Up Table (LUT), the hardpoint measured forces have been minimized. The “rule of thumb” for the LUT is that we should expect about 1/1000 correction. Our mirror weighs 170,000 N. We should expect to get within 170N. It looks like we are within this range.

    Pending tasks: To further improve the LUT, tests could be performed to validate that we have reached convergence and the LUT includes all the gravitational loads dependency. Merge latest version of technote into main, technote format is old.

  • SITCOMTN-092 M1M3 Force Balance System - Inertia Compensation

    Results: After applying different forces at 10% to 100% performance, maximum are occasionally seen at above 1000N, whereas the limit currently stands at 900 N.

    Pending tasks: Update technote to reflect most recent results (shown at the Glass Safety review) and merge into main. Define next steps, and possible risk minimization. Technote format is old.

  • SITCOMTN-107 M1M3 Actuator Delays and Following Errors

    Results: For aggressive slews, the measured forces do not track the applied forces well at all. So it appears that the problem with large hardpoint forces for the aggressive slews is more serious than just time delays.

    Pending tasks: We need to understand why the measured forces are deviating so strongly from the intended forces.

Bump tests#

  • SITCOMTN-083 M1M3 Mirror Cell Bump Testing

    Results: Bump tests have been performed throughout several months. Map of failures per actuator were created, together with typical failure modes (mostly on Z axis), for ~200 N bump tests. Actuators showed a higher failure rate when pushing the mirror up, with larger deviations in the positive direction. Importantly, for failed actuators no worsening trend over time was observed. Latency between actual and demanded forces was marginal. Forces overshot in 23% and undershot in 73% of bump test executions.

    Pending tasks: Establish a failure probability measure. Actuators passing the bump test may need to publish measured forces in the EFD for continuous monitoring, enabling early detection of potential failures. Additionally, define action plans based on the current data and requirements other than ‘not fault’.

Hardpoint tests#

  • SITCOMTN-081 M1M3 Hardpoint Oscillations During Elevation Slews

    Results: Evidence shown for oscillatory behavior during elevation and azimuth slews, by measuring hardpoint forces and identifying events above a 100 N threshold. Analysis of a one-off event started by TMA in June 2023 demonstrated no apparent coupling to M1M3.

    Pending tasks: Technote marked as current needs a review or update. Pending a more systematic analysis of slew events and identification of low amplitude oscillations at low elevation/earthquake behavior.

  • SITCOMTN-082 M1M3 Hardpoint Breakaway

    Results: Breakaway system works in general. Some notable exceptions (HP2, HP5 breakaway system faults at low (<30 deg) elevations, response shape also different) seem to be have an explanation according to Yijung and Petr.

    Pending tasks: Technote format is old and seems missing some discussion, conclusions, explanation of issues pointed out above.

Stability tests#

  • SITCOMTN-084 M1M3 Position Repeatability Analysis

    Results: The initial specifications on the mirror positions and rotations are not met, especially for the piston (z displacement). After discussion with experts, it was realized that these displacements are normal and correspond to the sag of the mirror cell due to gravity change that should be compensated by adjusting the M2 and camera hexapods. However this procedure does not seem to counteract the effect at the required level. For az only movements, the mirror displacements are within the specifications but for the rotation around the x axis where there are some outliers. The mirror rotation seems also correlated to the azimuth difference for movement < 50 degrees. For larger TMA movements the mirror rotation is within the specifications. Raise/park repeatability is verified as well.

    Pending tasks: Confirmation of the observed behavior with higher statistics. Study how to reduce the scatter for the correction in Z through adjustments of M2 and hexapods.

  • SITCOMTN-095 M1M3 Settling Time After a Slew

    Results: The requirement is failed using a threshold of 5 seconds after slew start due to a failure in the yPosition and yRotation columns predominantly, due to a slow drift of the cell. However, in a large majority of cases settling happens in < 2 s later and just barely misses the requirement for the system. NB that we have included RMS and bias of the IMS value, despite not being strictly the specification, as we considered it relevant to highlight these slow drifts that may not incur in any jittering at all.

    Pending tasks: Repeat analysis with updated adjustments to commands (which could be fixing the errors) when mirror is in place.

  • SITCOMTN-109 M1M3 Analyze position and rotation stability throughout a tracking period

    Results: After analyzing all the two-night tracking we have seen that the mirror remains stable. The duration of the tracking is 42 seconds and not 30 seconds as initially indicated.

    Pending tasks: Figure out what is going on with the 42 s ‘observing’ period.

Requirements#

For all the tests, the requirements are extracted from the following document:

  • LTS-88 M1M3 Mirror Support Design Requirements Document